| 1a The parking
brakes on the drivers side were a solid piece of rust, I had to beat off the
brake shoes with a hammer to get the parking brake assembly off the drivers
side. The passenger side parking brakes were missing. The parking brake cables are rusted solid. I haven't
fixed this yet, it requires a stainless steel parking brake kit. |
| 1b Ordered the
SS kit on the 27th of April along with both door pillar weatherstrips and a
ragtop pillow, details and pics once I get it back from #10c below.
Installed the kit on April 11th, everything went pretty well, but I forgot how
hard it is to put parking brakes on a vette. The cable that connects to
the brake handle was large in diameter than the original and it required
drilling out the guide slot to 3/16" instead of 1/8". |
| 2 The ground
wire for the wiper motor and heater fan motor was connected to the main starter
lug. The previous owner had run an individual ground to each item, but
apparently it had been hooked up wrong for a while because it melted the
shielding off the main power feed wire. The state of the wiring under the
hood was pretty lousy so I pulled the wiring off the starter and replaced all
the wiring under the hood, following color and size as closely as
possible. I went ahead and ran an auxiliary power feed also and installed
a relay to run my after-market electrical components. |
3 The paint on
the rims was lousy and the spare rim was a piece of garbage. I took all
four tires off and sanded the rims down to the base, they had multiple layers of
paint and quite a few runs. I used a grinder, files, and lots of sandpaper
but finally got them down to a good smooth surface, one of them was a bit too
rough to ever get it right, so I bought a new wheel and used this one for the
spare. I painted the insides with high-temp gloss black and the outsides
are the correct rally silver. |
4
All of this was done without me having successfully driven it once. I
ordered a carburetor the day I got it home. The carburetor on the car was
a Holley 3310 with vacuum secondaries and the choke was rigged up with a paper
clip. I really don't like vacuum secondary carbs with manual transmissions
so I decided to replace it with a Demon Carbs SpeedDemon 750 with mechanical secondaries
and electric choke. The problem with the carb was actually the fuel pump,
whoever built this engine put an electric fuel pump on without a regulator (or
filter for that matter) and the 11lbs of pressure blew out the seat
gaskets. While I was waiting for my Holley Blue series electric fuel pump
and regulator (which I traded my old carb for) I also figured out that the pump
was mounted badly, i.e. on the passenger side head, and the few times I was able
to drive it I had vapor lock problems, this may have also contributed to the
carburetor issues. Just for the coolness of it, I put an inline fuel
pressure gauge on the fuel line assembly. As you can see, someone strapped
the fan shroud up with wire ties, I bought the correct bracket and fixed this. |
5 The tach
cable was shot. The cable shielding was good, so I bought a new cable,
pulled the cable out of the shield and slid the cable into my existing
shielding, this necessitated taking the dash apart to get to the tach side of
the cable. While I had the dash out I discovered the car was originally
blue with a saddle interior, the dash and door panels were died black, but the
back sides were still saddle. I also used this as an opportunity to rip
the POS aftermarket stereo out and throw it away. Also I replaced the console data
plate with a shiny new one and replaced the leather steering wheel cover.
I have yet to get a replacement stereo, yet another item on my list. |
|
6
Sometimes a car can be too original and when it comes to points, original
sucks. Just for fun I wiped the dust off my dwell gauge and tried timing
the car. I couldn't get the dwell anywhere near right, when I set it to 29
degrees the intake vacuum went way down. I looked and saw exactly what I
expected, the distributor cam was round, there was hardly a raised edge left on
it. This didn't really break my heart as I wanted to change to HEI
anyway. I bought a MSD Pro Billet Tach Drive distributor, and installed
the vacuum advance lockout kit (I forgot how much I hate snap rings). I
changed the springs and advance limit bushing to get a little more aggressive
timing curve. I coupled it with an MSD 6AL ignition and an MSD blaster SS
coil. I chose the passenger side fender well to mount these items.
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| 7 The deck lid
was improperly aligned and the fiberglass hinge points were trashed, I took this
to a local boat shop and had them rebuild the hinge points. I theorize it
was misaligned because someone put weather-strip on both the upper and lower
surfaces. This didn't help anything as the correct upper piece of weather-stripping
was hard and brittle. The rear compartment vent has a broken vacuum line
and is frozen up from lack of use. This is on my list but not a priority. |
 8
When I pulled off the ragtop I realized it has been neglected for years, the
frame was rusted out pretty bad and had many pits and notches from rust. The first thing I did was sand it all down, I had to use a grinder to get rid of
some of the rust build up. Then I filled in all the holes with JB Weld and
re-sanded the whole thing. Once the surface was smooth I painted the frame
gloss black. I bought a new stainless steel screw kit for the frame and
replaced all the fasteners. I took the car to a Hot Rod specialist about
30 miles away and had him put a new ragtop on (corvette central has the best
deal on a full kit with weather-strip and screws). After the replacing the
guide bushings and polishing the pin brackets and latch handles, the top is now
the best looking part of the car. |
| 9 The
weather-stripping is abysmal. |

10a
Now that I have a new ignition, new carb and new top, I'm ready to get it
road-worthy. I get a set of Taylor Spiro Pro spark plug wires and go
through the excruciating process of custom making all the wires. I fire it
up and take it for a little spin, it runs like a bat out of hell when I'm accelerating
but like shit when I'm not. So I check it out and it sounds like I've got
some lifters rattling. I don't have a junk set of big block valve covers
to cut holes in so I call the local speed shop and they tell me they'll adjust the rockers for
25 bucks. I take the car over and leave it. Then the bad news
comes. They adjusted the lifters but it was still missing, they ran a
compression test and found a stuck/burnt valve. So I tell them to pull and
check the heads. They find the exhaust valve on my #3 cylinder is stuck,
the valve springs are the wrong ones for the competition Magnum 270 cam and the
springs were shimmed to get them close to spec. The receipt I have for the
last owners head work shows work performed, just not performed well. All
the valve guides need to be replaced because quite a few of the valves are
"sloppy". Im not sure if the valve springs were replaced but
they aren't on any receipt I have, so either they just reused the old springs
and shimmed them or they used the wrong springs and shimmed them. Either
way, the car must have sit for quite a while because a few of my valve springs
were compressed. So to wrap up this long story, they cleaned up the valves
and seats, put in new valve guides, and new springs. Thankfully the bottom
half engine work was done by another machine shop, maybe it's right. |
 10b It turns
out, that I was blaming the wrong guy somewhat. Even though the springs
were wrong, the car did sit for an extended period and therefore the springs
were compressed and would have been even if they had been the right ones.
After replacing the valve guides and doing a valve job (on a set of heads with
less than 500 miles since the last one), the aforementioned speed shop started
the car and it still had lifter rattle. They pulled the valve covers and
connected a drill to the oil pump, with 70 lbs of oil pressure there was no oil
coming out of the push rods. So they deducted that the root cause of the
problem with the heads was probably the rear cam bearing being improperly
installed. |
 10c Since
they were quite backed up and in the hope of saving some money I took the day
off work and pulled the engine. Hot Springs Speed and Truck was kind
enough to let me use their tools and I spent about 5 hours pulling the
engine. There are a few positives to this disaster, first I was able to
pull the engine out and inspect the rest of the previous machine shop's
work. Even though I didn't get as far as the rear cam bearing (so
I haven't verified it was the real problem yet), the rest
of their work looked pretty damn good, they balanced the crank and connecting
rods, they installed a new double timing chain and a new gear, and the pistons
are new. The cylinder walls still look freshly honed, they spot welded the
oil pump pickup to prevent it from falling off as Chevy's are prone to do.
The lifters and push rods are new. It has a new clutch, pressure
plate and throw-out bearing. One negative was the gaskets, they apparently
didn't feel like using gaskets, they used a very sloppy amount of silicon, but
it doesn't matter since I have to replace them all anyway. |
 10d
Another
negative was the oil pan. In addition to being the wrong oil pan (also
missing the windage tray), it had a huge dent in it where they pounded a hump in
it to make it fit over the power steering control valve. I ordered a
replacement from GM and the four main bearing cap studs to install the windage
tray. Hopefully this will make the dipstick read accurately.
Also this gives me a chance to put the vacuum canister back on as it was removed
at some point and cannot be installed with the engine in the car. I
ordered an LS7 oil pan from my local Chevy dealer on April 30th, it showed up on
May 4th and I almost made the mistake of buying it on E-bay. It was
cheaper direct from GM. This oil pan is a big improvement over the POS
pictured above. When I installed the engine with the new correct oil
pan it was necessary to take off the power assist arm. Five
minutes worth of additional work to do it right. |
| 10e When the
speed shop had my heads off I stopped by to look at the head work, and we
looked at my intake and discovered the damn thing was rectangular port and not
oval port. So I had yet another thing to replace. After taking some
measurements I determined that I wanted an Edelbrock Air-Gap RPM oval port
intake and I bit the bullet and ordered it. Whoever the previous owner had
rebuilding this engine was obviously smoking crack as they don't know anything
about air-flow or fuel pressure. |
11a Well today
(5/8/2004) I finished up what I started Thursday (5/6/04). Thursday I put
the engine back in the car. When I was done I still needed to mount the
radiator, stick the distributor, install Z-bar, water pump, power steering,
alternator. Today I arrived at the speed shop and started wrapping it up.
After adding the finishing touches we fired it up and it sounded
wonderful. It purred at an idle and had great throttle response. I
still need to put the hood back on and burp the engine (remove air from coolant)
and install the SS parking brake kit from 1b. Im doing this now because I
need to bleed the brakes after taking the brake booster off to install the
vacuum canister, and I figure I might as well do all the brake work at
once. While bleeding out the brakes on 5/12/04 I got as far as the front
passenger caliper, then the bleeder broke off in the caliper, we drilled it out,
used a left hand extractor, heated it with an acetylene torch, all to no avail.
I drove down to the auto parts store and traded in my caliper. It really
wasn't worth all that effort as it was leaking like a sieve. Then I got
back and the fitting on the brake line snapped off. This necessitated
another trip tot he store to get some 3/16" brake line and a compression
fitting. I don't like splicing but it will do until winter when I plan to
do a frame-off. |
| 11b Well I brought the
car home on May 16th, to wrap it up I had to fix a power steering hose
leak. The low pressure fitting needs some pipe tape. The car runs
pretty good, it still needs some tuning, but its good enough to enjoy for
while before messing with that. |
| 12 The
"Stingray" logos had no speed nuts, the rear bumper brackets are
missing and both rear quarter panel bumper bolts are missing. The speed nuts are
fixed, the bumper will have to wait. |
| 13 The carpet
is trash. Needs replacing. |
| 14 Both door
panels are borderline trash, need replacing. |
| 15 Both door
springs were broken/missing, they've been replaced. |
| 16 The
passenger vent knob is broken and not attached to the cable. Some of the
fiber-optic light indicators don't work. |
| 17 The clock is
stuck (no big surprise). |
18 Some of the
welds were broken on the driver side header, I had an exhaust shop pull it off
and re-weld. Apparently the automotive genius that built the engine just
jammed the header in and didn't care it he broke the welds. When
performing #10c above, I pulled the headers again and painted them with
high-temp (1200 F) black paint. |
| 19 The wiper
door is stuck (needs to be cleaned and lubed) and the vacuum and wiper fluid
hoses are in a state of disarray, the washer solenoid valve is broken and needs
replacing. I took out the wiper door assembly on 5/21/04 and lubed it up
good, I replaced the seal on the actuator and I may need to get the door bolt
holes rethreaded. Im trying to track down a correct wiper motor for this
car now. |
| 20 The oil
dipstick and tube were incorrect so I ordered an original set. Even with
the original set, they didn't read accurately, see #10c above.
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